Joined: Aug 2017 Posts: 112 Threads: 5
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Have made a start on slicing the early block, but the 24tpi blade In the bandsaw is too fine so after breaking one, after putting too much pressure on it, am now waiting for a much coarser 10/14 to use.
This is how far I've progressed, and quite an eye opener it is:
Geoff - Photos of slices to follow plus video using the new blade when it arrives.
Joined: Aug 2017 Posts: 641 Threads: 29
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How do we reduce a photo size ,please.
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Location: Essex
20-11-2017, 02:11 PM
(This post was last modified: 20-11-2017, 02:13 PM by Nick Lettington.)
Wow... That certainly helps understand how they end up porous!
Nice through-studs too btw.
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Nice photo of the mag crankcase. Where did you get the mod for oil inlet pipe? Are they available?
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25-11-2017, 04:13 PM
(This post was last modified: 25-11-2017, 04:28 PM by Tony Betts.)
[attachment=1430]Just found some of the cut up block parts from the NEW blocks I had made.
Might be helpful to show differences in water flow in new over old parts.
[attachment=1431]
[attachment=1432]
[attachment=1433]
[attachment=1434]
The last two pictures show the importance of proofing an item.
We had to do 18 changes to the pattern, and the casting pattern and box had to be totally remade 3 times to make the casting work.
However the difference in new and old blocks was clear, mainly due to there being no corrosion in the water jacket.
The first race car that had our new block fitted, on its first run out. Stopped the radiator from loosing half its water over 3 laps. And knocked 1 1/2 seconds of the cars best ever lap time. Even though the car had an electrical problem, and revs were limited to 6000rpm.
The improvement to the car from the new block, was down to the engine running cooler. So the bores were not bulging from poor water circulation, and bad heat transfer. It was run with same piston type, wich is our slipper Pistons. These Pistons run at a lower friction rate.
Hope all this helps and makes sence. Tony.
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Highly impressive Tony - b***s of steel to take on a project like that!
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Hi R,
I know it won't matter to many.
But when I first made the blocks, the out lay was enough to almost put me out of business.
Stock on the shelf was running down wilst I payed for everything. Including the first 30 to be made. And as the proofing took so long before I could take any money in. I was under a lot of pressure.
Trust me when I say, this was the time in my life I turned grey. And started to go bald.
ALOT OF STRESS.
Tony.
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I can only imagine Tony - as I said, impressive!